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| | #1 (permalink) |
| Resident Idiot | Code 42 driving me nuts... I keep getting intermittent problems seemingly related to the ignition system. My GN has a miss at part throttle and an occasional Code 42. It's hard to pinpoint what is happening because sometimes the car drives around perfect and then other times it goes into its fit. It seems like if you turn the car off and then turn it back on the symptoms go away until next time. The symptoms are part throttle miss, occasional code 42, bucking, changed exhaust note and sluggishness due to the timing switching in and out of some default value in the IGN module. Over the weekend I used this troubleshooting chart at Steve's site: http://www.vortexbuicks-etc.com/code_42.htm Here is my technical question: On step 4 of the above test, when I test the resistance from 'B4' to ground while applying 12v to 'D5' I am only measuring ~4600ohms, not 8000ohms like the chart states. I am wondering how critical this is and what the 8000ohms really means. I have tried 2 different ignition modules and currently I am using a brand new Wells Garner from the parts store. I am also using a known good coil pack but I am not sure if that could even be an issue here. I installed a wire loop in place of the Translator timing wire so the harness is essentially back to stock for test purposes. The B4 wire and D5 wire check out fine and are not shorted, open and they don't have high resistance. The chart basically leads me to 'check for intermittent connections' and I have. Needless to say I am stuck and at this point I guess I'll just start throwing more parts at the problem like plugs, wires, more coil packs, EST modules, cam sensors and maybe even the rear bumper. Anyone been through this troubleshooting chart before with similar results? Thanks,
__________________ Check Out MikesStuff4Sale.com to view my used parts! ![]() ------------------------------------------------ 1987 Buick Grand National Budget 4.1, 204/214 cam, TA-49 Turbo, Stockish Heads, V4, MSD50's, TH DP, JayJackson 62mm TB, Translator plus Extender powered. 3680# with pilot ------------------------------------------------ 1993 Mazda RX-7 4.1 Buick Powered 11.20 @ 128mph (2.4 60')! |
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| | #2 (permalink) |
| Boost Sux my Wallet Join Date: Aug 2003 Location: Mississippi Gulf Coast area
Posts: 1,119
| 4 whatever reason I cant get the link to vortex to work on my end. But here is a few helps from my head Have you taken your ecm and checked the connections there?? Check the chip and calpac double check the connections in the ECM. Have you double checked your wires on the plug and tower ends to verify no corrosion etc or maybe they are just getting tired?
__________________ 87 GN (3480lbs w/me & 1/2 tank) GT3255E, ESP FMIC, Razors Alky, Turbosaver, TA Headers, THDP w/test, ATR crossflow, TT, 38's, hopped up trans, Pats 10" 3k l/u, QA1r's, UMI Ups (adj) and lows, HR bar, MT DR's .2003 G35 Coupe Blk on BLk, JDM Clears, 18's, Prem PKG, Lthr, Bose....wifes car 2005 Harleys : Wide Glide & Duece ...Mucho Bling |
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| | #3 (permalink) |
| Registered User Join Date: Sep 2000 Location: Connecticut, USA
Posts: 6,431
| Have you gotten the code since you bypassed the timing control wire? Over at Full Throttles tech. website there's some code 42 fixes for certain translator boxes. I've never found mine but I'm thinking it's more the translator/chip than the wiring or module. I get the code about 6 times a year, it's a pain to reprogram the chip and clear it but it runs great after doing so. Mine won't go into boost at all when it shows up it runs crappy, driveable but no boost and power beyond 0, and the service engine light comes on at that point too which is kinda odd, it's like a 0 boost switch and light. And yes I'd check the chip socket connections too. I'm going to try another ECM someday when I get another one modified for LO-Z injectors. |
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| | #4 (permalink) |
| Resident Idiot | I haven't gotten the code since bypassing the T+ timing wire, but that was just done Saturday. It will started missing at part throttle yesterday and acted like it was going to code. I was disgusted with the car and just parked it because I thought after all the troubleshooting over the weekend and cleaning of the connectors I would have it licked. If I would have drove it around more I am sure it would have coded eventually as the symptoms were exactly the same right before it would throw the code.
__________________ Check Out MikesStuff4Sale.com to view my used parts! ![]() ------------------------------------------------ 1987 Buick Grand National Budget 4.1, 204/214 cam, TA-49 Turbo, Stockish Heads, V4, MSD50's, TH DP, JayJackson 62mm TB, Translator plus Extender powered. 3680# with pilot ------------------------------------------------ 1993 Mazda RX-7 4.1 Buick Powered 11.20 @ 128mph (2.4 60')! |
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| | #5 (permalink) |
| Resident Idiot | Oddly enough, my other car with the same chip, ECM, Translator, injectors started doing the same thing. Intermittant code 42's, studdering, popping through the exhaust and I can tell it was driving around with the wrong timing. That is for another thread and another day, but may be related. I have had some bad luck with exhaust leaks and ignition on these cars. ![]()
__________________ Check Out MikesStuff4Sale.com to view my used parts! ![]() ------------------------------------------------ 1987 Buick Grand National Budget 4.1, 204/214 cam, TA-49 Turbo, Stockish Heads, V4, MSD50's, TH DP, JayJackson 62mm TB, Translator plus Extender powered. 3680# with pilot ------------------------------------------------ 1993 Mazda RX-7 4.1 Buick Powered 11.20 @ 128mph (2.4 60')! |
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| | #6 (permalink) |
| Turbo Buick Vega Nut! Join Date: Feb 2004 Location: Weatherford, TX
Posts: 271
| Could the ESC itself be bad? When I had the Code 41 it turned out to be my cam sensor cap.
__________________ Dave English "V-6 Vegatex" Project: '77 Vega HB '84-'85 Hot Air Turbo/SFI Conversion Weatherford, TX denglish@ipapilot.org |
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| | #7 (permalink) |
| Registered User Join Date: Oct 2005 Location: Albuquerque NM
Posts: 55
| Are you running direct scan? When I used direct scan with a unshielded cable my car would code 42 and miss and buck at high boost. As soon as I put on a newer shielded cable all problems went away.
__________________ 87 GN, walbro 340, afpr, power plate, 60# injectors, PT67 P trim, Precision stock mount IC, 3500 stall West Coast 10 inch converter, Hooker (no cat), LS1 maf with translator, Turbotweak 100 oct chip, THDP. |
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| | #8 (permalink) |
| Resident Idiot | No Direct Scan plugged in but the Power Logger is. The USB cable isn't even hooked up to the PL when the problems occur though.
__________________ Check Out MikesStuff4Sale.com to view my used parts! ![]() ------------------------------------------------ 1987 Buick Grand National Budget 4.1, 204/214 cam, TA-49 Turbo, Stockish Heads, V4, MSD50's, TH DP, JayJackson 62mm TB, Translator plus Extender powered. 3680# with pilot ------------------------------------------------ 1993 Mazda RX-7 4.1 Buick Powered 11.20 @ 128mph (2.4 60')! |
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| | #9 (permalink) |
| Registered User Join Date: Oct 2005 Location: Albuquerque NM
Posts: 55
| Not sure about the power logger, but mine would have problems even with cable not plugged into the laptop. The cable would basicaly act as an antenna and send RF interference into the ECM causing the problem.
__________________ 87 GN, walbro 340, afpr, power plate, 60# injectors, PT67 P trim, Precision stock mount IC, 3500 stall West Coast 10 inch converter, Hooker (no cat), LS1 maf with translator, Turbotweak 100 oct chip, THDP. |
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| | #10 (permalink) |
| Registered User Join Date: Feb 2004 Location: IL
Posts: 856
| My code 42 stopped after many hours on a Sun Machine, the darn cap would occasionally miss and cause the car to run in limp mode and throw a code. They showed me the screen after saving it and you could clearly see the one line was was lower. Worth swapping out cam sensors to see.
__________________ Mike 87GN T-Top down 423lbs. Rebuild #2, BLK/BL Paint w/Custom Metal Flares, VPE Stg 3 Heads, 210/215 Roller Cam, TA49, V2 w/Blitz Blow Off, Billet Drum/Input, PI 3400 5disc, T Brake, Inland 3.5" DS, KB Plenum/70mm TB, Razor's Post Turbo Alky Kit, Devils Pre Turbo Alky Kit, 60lb Inj, Denso 280 Pump,-8/-6 SS Fuel Lines, MBC, Pwr Plt, PTE Oil Relocator, Preluber, Z06 Maf, Translator, Volt Master, Poston Headers, THSS 3.5" DP/Test Pipe, SS 2.5" Y Pipe w/No Muffs, PST 2" Drop, Poly Bushings, Boxed Upper/Lower Arms, QA1 Shocks, Vacuum Converted, Aerospace 11" Brakes w/SS lines, Alum Drums, Polished Autodrags 15x8/15x10, Nitto 555R 275/60's |
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| | #11 (permalink) |
| Registered User Join Date: Nov 2005
Posts: 2,313
| Try reburning the chip. I've had some that were sort of *flakey* that would code 42 for no apparent reason. Burning the same code on another chip cured it.
__________________ "News is like hot soup, it's meant to be sipped. if you swallow a big mouthful, you'll get burned". "Some days, it's just not worth chewing through the restraints." |
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| | #13 (permalink) |
| NOS JUNKY Join Date: May 2004 Location: Claremore, OKLA.
Posts: 155
| I had BAD LUCK with the Wells ignition modules! I tried 2 in one week! BOTH JUNK!!!! I also tried a Echlin from NAPA and had to go back twice. I had many different symptoms from-would not start after driving(engine warm), part throttle miss, bucking at WOT, not reving over 3800 RPMs. I finally bought GM ignition module and coil pack. Kirbans is selling original coil packs for 59 bucks! Limited supply. I bought a spare cause the price is tough to beat! after installing them, the car run really good! On one of my other Grand Nationals, I found a bent prong on the module plug in. That car was missing BAD but straightening the prong cured that! Dan
__________________ 84 short wide 13.34@105 & 87 SS Monte 11.75@114 |
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| | #15 (permalink) | |
| Dr. Nehi Join Date: Feb 2003 Location: Philly area
Posts: 861
| Quote:
I also had a module that would get hot and intermittently produce the same results-- bucking, stumbling, sometimes with code 42, sometimes without. Tested fine when not hot, intermittent problem was a real PITA to find.
__________________ 1987 Buick Grand National 10.22@130.9mph (1.47 60') on E85 Mods: Bronsonian ported iron heads with stock valves, 70GTQ, Comp Cams 214/214 roller, Cotton's FMIC, 95# injectors, Aeromotive A1000, FAST XFI tuned by Dale Cherry, Cotton's 3.5" downpipe, 44mm Tial gate, ATR 2.5" exhaust, 9.5" Vigilante, Eaton posi, Moser 28 spline axles. | |
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