Only change was a TE-45a turbo. That thing is huge!
I quickly learned the 50# injectors were too small in combinaiton with this turbo.

. The injector duty cycle about 50 feet off the line was 108% and the car kept popping at a few points in the run.
The boost last night was 20psi, anything more and it would just pop. The car went almost the same exact MPH when I ran the TA-49 at 25.5psi.
No spectacular ET's to report as I was on and off the throttle when the popping was occuring. It did go 11.80 something @ 117.69mph.
I guess I really need some larger injectors afterall.
Another thing I noticed was the MAF was maxing out at 255gps on the lauch and once when I accidently twisted the bleeder valve a little too quickly! I only have a 30psi gauge so I am not sure how high it actually went, but it buried the gauge for a split second

. I may need the Extreme chip which will triple the resolution since mine is only doubled.
Wasn't the best night at the track but any night driving the car home is a good night.

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1987 Buick Grand National
Budget 4.1, 204/214 cam, TA-49 Turbo, Stockish Heads, V4, MSD50's, TH DP, JayJackson 62mm TB, Translator plus Extender powered. 3680# with pilot
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1987 Turbo T with 5,888 Original miles FOR SALE!
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1993 Mazda RX-7 4.1 Buick Powered
11.20 @ 128mph (2.4 60')!